It’s been awhile since my last post in this thread. I should have updated sooner because since then a lot has happened to my bike.
TL;DR version: everything works fine now.
In case this may serve as a diagnostic for other people I’ll expound on my experiences:
There were two major issues
(1) onboard charger wrongly detects an external power connection (read: charging indicator lights up).
(2) strange sounds from my drive train.
(1) onboard chargerA few days after the firmware update which (initially) solved to charging indicator issues, everything went south.
The next Monday (why is it always on Mondays?!?!) after the firmware update I was able to commute to my workplace without much issues but after work when I was about to go home, it took a LOOOOONG time before the charging indicator went out.
Before, the charging indicator wrongly lit up only for a few seconds … this time it took more than half an hour … and my bike hadn’t been plugged in during the entire workday.
When I was finally able to leave, the indicator was more often lit than not.
After about a 2~3 km (1.2~1.8 miles) the onboard charger made its final decision ... too bad it was the wrong one. The charging indicator kept being lit, so at the next crossroads when I needed to make a full stop I was stuck with an expensive brick on wheels. A heavy one because even with the ignition key removed, the controller was still active causing the electric motor to provide resistance while pushing my bike back to the secured parking lot of my work.
Before I started this workout, I tried resetting the BMS, toggling the ignition key, etc. … all to no avail.
On the display the error code 6 , 20 and 47 appeared.
To the credit of my reseller, they picked up my bike free of charge.
After contact with Zero, they decided to completely replace the onboard charger under warranty.
This replacement provided a lasting solution to the issue.
I don’t know if that’s by design or an indication of another underlying issue, but to this day I’m still having the same behaviour as explained in this thread:
http://electricmotorcycleforum.com/boards/index.php?topic=7553.0(2) Stranger SoundsAt the end of my previous post I mentioned a strange sound while breaking. Later I figured out this was only during regenerative breaking.
Over the next few weeks this sound slowly became louder and louder … again, only during regenerative breaking. I finally decided to take my bike back to the shop when two pedestrians were visibly startled by this sound when I happened to let go of the throttle when I was right behind them.
At the shop they found the cause and showed it to me … the damage was startling!
I’m sad to say I neglected to take a photo so I’ll try to paint a picture with words here.
The front belt sprocket, has square teeth on the inside which interlocks with the axle of the motor.
Ex:
https://catalog.zodiac.nl/ZodiacImage.aspx?image=ZDCE0476&format=Navigatie These teeth where almost completely gone, leaving behind only a jagged surface and the odd tooth left and right … which were also almost completely worn out.
The square teeth of the axle of the electric motor itself showed similar albeit much, much less damage.
It presume it would have taken only a few more twists on the throttle in Sport Mode to be stuck in the middle of the road without a working drive train.
Zero advised to do a complete replacement of the entire drive train.
Front and back sprocket, belt and even the electric motor since the axle itself is not a replaceable component in the motor.
Fortunately for me, this too, was replaced under warranty.
With this replacement all remaining funny sounds are gone and my bike now makes the same sounds compared to the ones I have on my helmet camera (when I did a few test rides at resellers) and listening to other Zero's on reviews on YouTube.
My reseller told me that Zero had never before seen this kind of damage, they certainly didn't expect this on a new bike with only 3000~4000km (1800~2500 miles) on the odometer. So contrary to normal procedure where they just write off the components, they asked to send the drive train back to them for further investigation.
… Too bad because I would have liked to have built something at home with a 52kW 3-phase generator. For my purposes, the damage there was to the axle was of little consequence anyway.
edited to add: with the replacement of my drivetrain I get about 10~15% more range out of a charge
Conclusion:These two issues must have been present from the first day I took the bike out of the shop. It took a while for everything to first get recognized by the shop and then get fixed, but I had no more issues since.